The New Arm

We’ve learned a lot since Rutgers, and one of the biggest things was how to push down the ramp with less error. We switched to a system of using a metal fin to wedge down the ramp rather than pneumatically pushing the ramp down because it was a lot more Read more

Crash

So in the last match, our robot’s battery failed right in front of the Coopertition bridge. Another team tried to get onto the Coopertition bridge so that the alliance could still score Coopertition points, but, with the way our drive train was designed, our robot couldn’t be shoved. Their robot, Read more